Thinking teardown

Disclaimer: Links on this page pointing to Amazon, eBay and other sites may include affiliate code. If you click them and make a purchase, we may earn a small commission.

Road Trip

Supporting Member
Supporting Member
Joined
Jul 8, 2023
Messages
1,669
Reaction score
4,740
Location
Syracuse, NY
Hi Roadtrip; You have helped me in the past when I was looking at ecm as possible culprit and your wiring diagrams and detailed information were extremely helpful.

Hello Anchor,

Glad to hear that you found the previous efforts helpful. Common problems can often be fixed by throwing a
set of fresh plugs at the motor. Given the troubleshooting effort you have put in to date, this has the look &
feel of an Uncommon problem. :0) But with a disciplined troubleshooting approach we should be able to take
this problem pie and at the very least figure out what are the good 7 slices vs the remaining bad slice. (ie: I believe
that the SBC is a proven design, follows the laws of physics, and we just have to figure out where your specific
engine deviates from the formula that is known to work in millions and millions of engine bays in the real world.)

Disclaimer: I have troubleshot my entire career, but at the same time I'm still learning this remote troubleshooting
thing. I never realized just how much better it is to have your head under the hood as opposed to studying photos
and typing thoughts in coherently. Doing this remotely feels as clunky as trying to properly share the experience
of watching the movie '2001' using Morse Code. A lot seems to be lost in the translation. :0)

But if you are willing to sort this out in public, so am I. Fortunately for us, there's lots of talent in the audience
who can jump in and keep this moving in the right direction.

****

So with the disclaimer out of the way, let's step through the detailed current status you shared:

I have timed this engine so many times I fear I may have to buy a new bulb for timing light. I set it at 0 and mark has been steady as can be with the ecm wire disconnected.

What you described (a steady 0° with the ECM wire disconnected) *is* expected behavior. I'll go
a step further, and tell you that if you didn't have a steady reading with the ECM disconnected then
we would have to stop here and figure out where the slop (spark scatter) was coming from.
(Bad timing chain, excess knife-edge wear in the cam/dizzy gears, excess vertical up/down travel
allowed in the dizzy shaft, or excess clearance/play in the dizzy bushings.)

In English, a steady 0° reading with the ECM disconnected is no small win. Let's keep that in the back
of our mind and proceed to the next step.


Then when I re-connect the wire my mark jumps up to a ways before the timing indicator, maybe 12 or 14 btdc and it constantly jumps around a few degrees, maybe up to 5. I assumed this was ecm doing it's job but that may not be the case.

This is also expected behavior. IF the timing remained at a steady 0° when you
reconnected the wire we would have to stop and troubleshoot that. (Open wire
in the harness, ECM not responding, etc.)

Again, this is a win in my book. A feature, not a fault.


When I first was troubleshooting the truck I had 0 compression in #8. When I pulled valve cover, I believe the exhaust valve was open and the spring compressed. I couldn't imagine the valve spring not expanding and closing the valve. It also got me thinking that it had damaged that hydraulic roller lifter. But i loosened up, checked the pushrod and re-set valves. All seemed to be ok after. I even wondered if po had missed the lifter when he stabbed the pushrod but that didn't seem possible due to the small pushrod hole in head. Was the only other possible cause the valve terribly tight in the guide and it freed up when I loosened it and reset lash? (Don't know if lash is proper term with hyd. lifters).

OK, now we are entering an illegal condition in the mechanical realm. A valve stem with enough friction
between itself and the surrounding guide that a stock SBC spring with the following specs (80 lbs
at installed height, ~200 lbs at full lobe opening) couldn't close it, then that's no bueno.

Given the spotty operational history since this engine was put together (plus the fact that at
least 2 other owners have tried to sort this out) ...I'm in agreement with the others that we
need to label this valve stem/valve guide area as suspected bad, and you have to do what it
takes to prove to yourself that the clearances meet factory specification in this area. (!)

(EDIT)
This is purely hypothetical, but if the exhaust valve had been (mis)adjusted at some point
to where the exhaust valve and piston tried to share the same space at the same time, then
it's entirely possible that the exhaust valve stem was bent/distorted just enough that
it was jammed into the valve guide? Remember the valve spring pressure against the
retainer is anywhere between 80-200 lbs, so finding the valve stuck open tells me that
there's a problem in this area...even if it did free up. No telling if the 'sticktion issue'
doesn't try and return once the valve heats up and expands during normal operation,
sticks in the process, and causes misfires in this suspect cylinder, leading to a false-lean
reading by the O2 sensor, which richens up the A/F mixture, giving you both rough running *and*
poor MPG to boot.

NOTE: The vast majority of valves that fail/drop their head into the cylinder were whacked
at some point prior to the failure. Stress fractures + thermal cycling = failure.
If you were my neighbor I would be starting the 'let's remove the cylinder heads as a safety
precaution and find out what's going on' sales job. I'd rather take the chance of removing
the heads and finding zero issues with the values as opposed to telling you that all is well,
only to have the suspect freed-up exhaust valve either continue to cause the driveability/MPG
issue at best, or worst-case, completely fail, possibly taking the piston/rod/block/head with it. (!)


I have struggled with this so long I think the people who are aware of it have written me off as a window licker. I ordered and installed a new knock sensor and after reading of overtightening problems I actually torqued it in I believe at 15 lbs. By the way the snapon shows no knocks but I can get them by tapping on the engine.

OK. The Snap-On shows no knocks while driving but you can get them by tapping on the engine.

Excellent! This is a troubleshooting win, right up there with the steady 0° reading
with the wire disconnected and the ECM taking active control of the spark advance
once it's reconnected. We are tightening the problem description with proving what's
good.


Valves have been quiet and no popping. Interesting note, to me at least. I was messing around the other day and tried to adjust #1 rockers while running. When I put a deep well socket on the lifter adjusting nut the engine wanted to die. I had not turned it yet, just set the socket in place. Tried to place it on another lifter and same thing. Have done this a million times with flat tappet cams and no problem, just go ahead and adjust. Is this something to do with roller lifters?

Good question. The short answer is no, for properly operating hydraulic flat tappets and hydraulic roller lifters are the
same internally
in the area where you are trying to get the lifter preload into the designated window. (1/2 to a full turn
past the start where a loosened/clattery lifter goes just quiet.)

Sounds to me that the valve preload is currently set so deep that any
further downward pressure at the rocker arm ball is enough to hold the valve
just enough off the valve seat that this cylinder starts to misfire. (Most people
don't realize that a 250hp V8 throttled down to only make ~5-7hp at a hot idle
is a pretty fragile internal combustion balancing act, easily disrupted.)

To me, both the sticky valve you discovered AND the too-easily disrupted
valvetrain both indicate to me that one of the POs must have had the valves
set way too tight. And when the valves in the head are off, they can be super
difficult to troubleshoot unless you have some hard-won experience in this area.

Good on you for being so observant, for I think this will be the key to eventual
success in this engine bay.


That stuck #1 lifter has troubled me since I found it. I can't see how valve spring would not have overcome it. I will re-install plugs and mess with timing as you suggested. I'd much rather not have to tear down but I have months in this off and on and sure need to find it. I truly appreciate those of you chiming in as I have reached the point of trying the same ideas over and over and hoping for different results. Will reassemble stuff and do some timing adjusting tomorrow. Thank You.

You are in good company, for I have also lost confidence in that valve that you discovered
hung/stuck open. Thinking about this, a valve that was properly adjusted could only
stick somewhere in the normal lift. Assuming for a second that the preload was set
properly but the valve stem guide was too tight, then the valve would have stuck
somewhere in the normal lift area, and the chances of piston/valve contact would be
slight.

But IF whoever assembled the engine way overtightened this particular exhaust valve, then
piston/valve contact would be a much higher probability, and I can see this being wounded
right out of the box, and never drove quite right from the first mile after the rebuild?

**** Where do we go from here?

1) If at all possible, I would recommend that you minimize how much this vehicle is driven in
order to avoid sudden failure of a previously overstressed part. (ie: The valve you found stuck open.)

2) Get the engine running, and since you are sitting at 0° base (initial) timing, add 4-5° degrees of
advance and see if this doesn't improve the drivability. If it does, let's remember this for after
you reinstall the heads.

2A) Or you decide to just go ahead & pull the heads at this point...and experiment with the ignition
timing after reassembly.

3) Time to stop poking around the edges. Given all that we know at this point, a normal tuneup or
sensor replacement isn't going to fix what you've observed. Pull the heads, and get them to a
SBC-savvy machinist. Explain the history to him. In an abundance of caution, be sure to identify
the valve that you discovered hung open, and ask him to retire it from service.

What you want from this machinist is all 16 valves moving freely in their guides, and providing a
positive seal when sitting on the seat. The better machinists are pretty exacting about all this,
hopefully you can find one of the better ones. (I've had my best luck with word of mouth. If you
know any local racers, they usually know which machinists are the wizards as well as the duds to avoid.)

4) Put it all back together, and methodically assemble the valvetrain and set the preload. Once the
engine is started, set the initial timing at 4° BTDC and let the functioning KS alert you if this is
a good or greedy setting. Since the combustion chambers are carbon free, I'll bet that it runs
smooth & sharp.

****

That's plenty enough for now. Like I said at the beginning, there are common problems that are
easily sorted out, and then there are the Uncommon problems that require us to dig a little deeper.

I'm assuming that you were able to buy this truck at a discount because the engine was part of the
problem instead of part of the solution. Even so, I am confident that this *is* fixable. The engine
isn't overheating, you didn't mention any noises, the ignition & ECM seem rational, etc.

But the engine runs rough and gets poor gas mileage. Both of which could be explained by the
valve getting whacked hard enough that an 80-200 lb. spring couldn't close it. (By the way, due to
hyperextension/misadjustment the interference fit might present at .600" lift, but since your cam only lifts it .480",
once you got it to close it hasn't been pushed all the way back out to the bad spot. This would help to
explain why the problem hasn't reoccurred since.)

Anyway, I share the above as food for thought, not a guaranteed diagnosis. I see that Schurkey has beat me
to this. It's my sincere hope is that we've independently come to the same general conclusion. :0)

Best of luck. And let's document this fix for those who come here troubleshooting similar GMT400 powerplants
that are resisting repair.

Cheers --
 
Last edited:

Anchor

OBS Enthusiast
Joined
Dec 9, 2023
Messages
64
Reaction score
67
Location
Oregon
Yup, valves can get stuck, and the spring won't pop 'em free.

This does the valve and the guide no good whatsoever; and if the piston hits the open valve, there's trouble in paradise.


Lucky.


"Lash" refers to a specific clearance in the valvetrain. Hydraulic lifters generally run with preload, so the word "lash" wouldn't apply.

You re-set "lifter preload".


Sounds like the rocker adjustment is so tight that it's on the verge of holding the valves open. Any additional disturbance on the rocker/valve results in the valve not sealing.

You may have adjusted the valves multiple times, but if the lifter preload is too tight, it's too tight. One wonders what would happen if the rockers were backed-off half a turn. Or backed-off until each one clattered, and then re-tightened an appropriate amount.
 

Anchor

OBS Enthusiast
Joined
Dec 9, 2023
Messages
64
Reaction score
67
Location
Oregon
Hello Anchor,

Glad to hear that you found the previous efforts helpful. Common problems can often be fixed by throwing a
set of fresh plugs at the motor. Given the troubleshooting effort you have put in to date, this has the look &
feel of an Uncommon problem. :0) But with a disciplined troubleshooting approach we should be able to take
this problem pie and at the very least figure out what are the good 7 slices vs the remaining bad slice. (ie: I believe
that the SBC is a proven design, follows the laws of physics, and we just have to figure out where your specific
engine deviates from the formula that is known to work in millions and millions of engine bays in the real world.)

Disclaimer: I have troubleshot my entire career, but at the same time I'm still learning this remote troubleshooting
thing. I never realized just how much better it is to have your head under the hood as opposed to studying photos
and typing thoughts in coherently. Doing this remotely feels as clunky as trying to properly share the experience
of watching the movie '2001' using Morse Code. A lot seems to be lost in the translation. :0)

But if you are willing to sort this out in public, so am I. Fortunately for us, there's lots of talent in the audience
who can jump in and keep this moving in the right direction.

****

So with the disclaimer out of the way, let's step through the detailed current status you shared:



What you described (a steady 0° with the ECM wire disconnected) *is* expected behavior. I'll go
a step further, and tell you that if you didn't have a steady reading with the ECM disconnected then
we would have to stop here and figure out where the slop (spark scatter) was coming from.
(Bad timing chain, excess knife-edge wear in the cam/dizzy gears, excess vertical up/down travel
allowed in the dizzy shaft, or excess clearance/play in the dizzy bushings.)

In English, a steady 0° reading with the ECM disconnected is no small win. Let's keep that in the back
of our mind and proceed to the next step.




This is also expected behavior. IF the timing remained at a steady 0° when you
reconnected the wire we would have to stop and troubleshoot that. (Open wire
in the harness, ECM not responding, etc.)

Again, this is a win in my book. A feature, not a fault.




OK, now we are entering an illegal condition in the mechanical realm. A valve stem with enough friction
between itself and the surrounding guide that a stock SBC spring with the following specs (80 lbs
at installed height, 200 lbs at full lobe opening) couldn't close it, then that's no bueno.

Given the spotty operational history since this engine was put together (plus the fact that at
least 2 other owners have tried to sort this out) ...I'm in agreement with the others that we
need to label this valve stem/valve guide area as suspected bad, and you have to do what it
takes to prove to yourself that the clearances meet factory specification in this area. (!)

(EDIT)
This is purely hypothetical, but if the exhaust valve had been (mis)adjusted at some point
to where the exhaust valve and piston tried to share the same space at the same time, then
it's entirely possible that the exhaust valve stem was bent/distorted just enough that
it was jammed into the valve guide? Remember the valve spring pressure against the
retainer is anywhere between 80-200 lbs, so finding the valve stuck open tells me that
there's a problem in this area...even if it did free up. No telling if the 'sticktion issue'
doesn't try and return once the valve heats up and expands during normal operation,
sticks in the process, and causes misfires in this suspect cylinder, leading to a false-lean
reading by the O2 sensor, which richens up the A/F mixture, giving you both rough running *and*
poor MPG to boot.

NOTE: The vast majority of valves that fail/drop their head into the cylinder were whacked
at some point prior to the failure. Stress fractures + thermal cycling = failure.
If you were my neighbor I would be starting the 'let's remove the cylinder heads as a safety
precaution and find out what's going on' sales job. I'd rather take the chance of removing
the heads and finding zero issues with the values as opposed to telling you that all is well,
only to have the suspect freed-up exhaust valve either continue to cause the driveability/MPG
issue at best, or worst-case, completely fail, possibly taking the piston/rod/block/head with it. (!)




OK. The Snap-On shows no knocks while driving but you can get them by tapping on the engine.

Excellent! This is a troubleshooting win, right up there with the steady 0° reading
with the wire disconnected and the ECM taking active control of the spark advance
once it's reconnected. We are tightening the problem description with proving what's
good.




Good question. The short answer is no, for properly operating hydraulic flat tappets and hydraulic roller lifters are the
same internally
in the area where you are trying to get the lifter preload into the designated window. (1/2 to a full turn
past the start where a loosened/clattery lifter goes just quiet.)

Sounds to me that the valve preload is currently set so deep that any
further downward pressure at the rocker arm ball is enough to hold the valve
just enough off the valve seat that this cylinder starts to misfire. (Most people
don't realize that a 250hp V8 throttled down to only make ~5-7hp at a hot idle
is a pretty fragile internal combustion balancing act, easily disrupted.)

To me, both the sticky valve you discovered AND the too-easily disrupted
valvetrain both indicate to me that one of the POs must have had the valves
set way too tight. And when the valves in the head are off, they can be super
difficult to troubleshoot unless you have some hard-won experience in this area.

Good on you for being so observant, for I think this will be the key to eventual
success in this engine bay.




You are in good company, for I have also lost confidence in that valve that you discovered
hung/stuck open. Thinking about this, a valve that was properly adjusted could only
stick somewhere in the normal lift. Assuming for a second that the preload was set
properly but the valve stem guide was too tight, then the valve would have stuck
somewhere in the normal lift area, and the chances of piston/valve contact would be
slight.

But IF whoever assembled the engine way overtightened this particular exhaust valve, then
piston/valve contact would be a much higher probability, and I can see this being wounded
right out of the box, and never drove quite right from the first mile after the rebuild?

**** Where do we go from here?

1) If at all possible, I would recommend that you minimize how much this vehicle is driven in
order to avoid sudden failure of a previously overstressed part. (ie: The valve you found stuck open.)

2) Get the engine running, and since you are sitting at 0° base (initial) timing, add 4-5° degrees of
advance and see if this doesn't improve the drivability. If it does, let's remember this for after
you reinstall the heads.

2A) Or you decide to just go ahead & pull the heads at this point...and experiment with the ignition
timing after reassembly.

3) Time to stop poking around the edges. Given all that we know at this point, a normal tuneup or
sensor replacement isn't going to fix what you've observed. Pull the heads, and get them to a
SBC-savvy machinist. Explain the history to him. In an abundance of caution, be sure to identify
the valve that you discovered hung open, and ask him to retire it from service.

What you want from this machinist is all 16 valves moving freely in their guides, and providing a
positive seal when sitting on the seat. The better machinists are pretty exacting about all this,
hopefully you can find one of the better ones. (I've had my best luck with word of mouth. If you
know any local racers, they usually know which ones are the wizards as well as the ones to avoid.)

4) Put it all back together, and methodically assemble the valvetrain and set the preload. Once the
engine is started, set the initial timing at 4° BTDC and let the functioning KS alert you if this is
a good or greedy setting. Since the combustion chambers are carbon free, I'll bet that it runs
smooth & sharp.

****

That's plenty enough for now. Like I said at the beginning, there are common problems that are
easily sorted out, and then there are the Uncommon problems that require us to dig a little deeper.

I'm assuming that you were able to buy this truck at a discount because the engine was part of the
problem instead of part of the solution. Even so, I am confident that this *is* fixable. The engine
isn't overheating, you didn't mention any noises, the ignition & ECM seem rational, etc.

But the engine runs rough and gets poor gas mileage. Both of which could be explained by the
valve getting whacked hard enough that an 80-200 lb. spring couldn't close it. (By the way, due to
hyperextension/misadjustment the bent part might be at .600" lift, but since your cam only lifts it .480",
once you got it to close it hasn't been pushed all the way back out to the bad spot. This would help to
explain why the problem hasn't reoccurred since.)

Anyway, I share the above as food for thought, not a guaranteed diagnosis. I see that Schurkey has beat me
to this. It's my sincere hope is that we've independently come to the same general conclusion. :0)

Best of luck. And let's document this fix for those who come here troubleshooting similar GMT400 powerplants
that are resisting repair.

Cheers --
Thank you Road trip. I think I will pull the top end off and take the heads in as you suggest. Your style of walking people through these headaches is much appreciated and offers me some encouragement. By the way, I did buy the truck at a great price and did so with the intent of putting a new motor in it till I realized what all was in the existing motor. Will get it pulled down in the next few days. I am wondering with the intake and heads off if it will easy to use dial indicator and make sure I don't have a bad cam lobe? I would really like to know what cam was installed and that lobes are still consistant. One way or the other I will pull it down this week and will certainly document and share what is finally found. I truly appreciate your knowledge and willingness to share it. Thank You.
 

Anchor

OBS Enthusiast
Joined
Dec 9, 2023
Messages
64
Reaction score
67
Location
Oregon
Yup, valves can get stuck, and the spring won't pop 'em free.

This does the valve and the guide no good whatsoever; and if the piston hits the open valve, there's trouble in paradise.


Lucky.


"Lash" refers to a specific clearance in the valvetrain. Hydraulic lifters generally run with preload, so the word "lash" wouldn't apply.

You re-set "lifter preload".


Sounds like the rocker adjustment is so tight that it's on the verge of holding the valves open. Any additional disturbance on the rocker/valve results in the valve not sealing.

You may have adjusted the valves multiple times, but if the lifter preload is too tight, it's too tight. One wonders what would happen if the rockers were backed-off half a turn. Or backed-off until each one clattered, and then re-tightened an appropriate amount.
Thanks Schurkey; Your points are well taken. I am at least going to pull intake and heads and get the heads checked out by machine shop. Your input is always paid attention to and appreciated. I will always be a novice at these things but damned if I will give up. You guys keep me going. Will probably back off all of the lifters 1/2 turn just for the heck of it and give it a whirl before tear down.
 

Anchor

OBS Enthusiast
Joined
Dec 9, 2023
Messages
64
Reaction score
67
Location
Oregon
Will proceed with the work on this truck later in the week. Since this has run me in circles for so long I will be sure to follow up on what happens as I investigate. Thank all of you for the sound advice and I am very much looking forward to getting it ironed out and making it my driver. Thanks again.
 

Anchor

OBS Enthusiast
Joined
Dec 9, 2023
Messages
64
Reaction score
67
Location
Oregon
I am hoping that those of you who were helping me with my poor running problem will be notified of this post. I don't understand how the forum works exactly. Anyway, I pulled the engine and disassembled heads, pan, and pulled camshaft out. Here's what I found. It's a 383 stroker. 3.75 stroke. 0.40 pistons. Scat crankshaft. Approx. 4.03 bore. Motor appears to be like I thought and new looking. A little carbon on pistons but I think because I have idled it for hours in searching for problem. Block is a two bolt main stamped 5.7 LG SGI and 638 several places on block. Nice tight double roller timing chain. Cam is Comp cams 08-500-8 and cam and lifters look fine. Has the 400 style balancer with the shaved areas and flex plate is drilled and weighted. No shims on crank to flex plate. I can't find any evidence of relieving of rails. Does the Scat crank allow this? I will mic. the cam today but it and the lifters look fine. Somebody invested a bunch of money in this thing, way more than I paid for the truck. I realize that does not mean it's ok. When I had it up in the air I disconnected the flex to torque converter bolts and started to remove bell housing bolts. None were more than finger tight and the top one was almost out. I didn't look at the block to housing gap but think it must have been sagging. Obviously this has grown in scope but I would sure like to salvage what I have and take advantage of all the parts that have been thrown at it. Heads will go in next week to be examined over the sticking valve in #8 hole. I am almost wondering if the loose engine to transmission bolts were causing roughness that I mistook for missing. Any of you folks please feel free to chime in and direct me toward getting this solved. Now, as soon as I cultivate the garden and pressure wash the deck I will be right back at it. One more thing. When I removed the three flex plate to torque converter bolts they were painted up very nicely on the heads in green, white and red. What on earth? This paint is not just left over from previous life but good quality paint and intentionally done. What don't I know here? Thank you and will await your much needed input.
 

Schurkey

Supporting Member
Supporting Member
Joined
Jan 14, 2018
Messages
12,548
Reaction score
16,267
Location
The Seasonally Frozen Wastelands
0.40 pistons... ...Approx. 4.03 bore.
Kinda guessing it's bigger than .030-over if it's got .040-over pistons.

When I had it up in the air I disconnected the flex to torque converter bolts and started to remove bell housing bolts. None were more than finger tight and the top one was almost out. I didn't look at the block to housing gap but think it must have been sagging.
That can't be good.

When I removed the three flex plate to torque converter bolts they were painted up very nicely on the heads in green, white and red. What on earth? This paint is not just left over from previous life but good quality paint and intentionally done.
Was the flexplate and converter ALSO painted in matching colors? Maybe just a homegrown color code to keep the flexplate and converter aligned.

Or the previous owner's kid was having fun with Dad's spray-paint.
 

thinger2

I'm Awesome
Joined
Jul 6, 2019
Messages
1,682
Reaction score
4,274
Location
Tacoma
Looking here for guidance. I have posted multiple times about 92 K1500 Regular cab shortbed that I purchased in November. I have been through a diagnosis jungle since then. I have a good friend who is remote from me who has helped me try to troubleshoot, (he is smarter than me) by the way. It is is newly rebuilt motor, almost no miles, done around 2019 and I think at least 2 people ahead of me in trying to get straight. 190 compression all cylinders. Holds steady 19 to 20 in. vacuum. Idles great. Had an exhaust valve stuck open when I got it and thought for sure I had it fixed. Have been through the learning curve on sensors, injection, fuel pump, etc. etc. etc. It is a pretty much rust free Oregon truck and I intend to make it my daily driver with lots of work and even paint at the end.
Engine starts, runs ok but in accelerating and cruising speed it feels like a plug wire or 2 are off and fuel mileage is pitiful. It has, I think, a Comp cams Hydraulic roller and comp cams roller tip rockers that are squarely on the valve stems. After all of this I am thinking about pulling engine and removing cam to get the part numbers and inspect lifters and cam itself as well as look over heads, valve springs, etc. The cam does not really lope at all but I want to see that number and mic it to see if a problem. I have a cheap dial indicator but with hydraulic lifters I think it may be real hard to get an accurate lift reading. I do have a lift and cherry picker in my shop so at least it won't be done in terrible conditions. This thing has kind of defeated me and I don't need it to get to work. I acquired an MT 2500 during this project and it has not revealed the problem. No codes either other than when I have unhooked sensors. It is hard for me to look at this thing objectively, hence my asking this board, "What would MacGuyver do? Any help appreciated. I rebuilt my first smallblock in 1970 but am by no means a mechanic and understand that. I am happy to look at opinions and a lot of you folks are much more knowledgeable than me. I will monitor the forum for suggestions for several days before charging ahead. Thank You.
I think you need to go back and take another real hard look at that stuck exhaust valve first.
How did you determine that it was stuck?
What did you do to un-stick it?
A compression test only tells you what is happening at starter rpm.
It does not tell you what is happening at 4 thousand rpm.
Could be a cracked lifter that blows oil at pressure or sticks in the bore.
Could be a bent valve that only hangs when its hot or only hangs at the end of its travel.
Could be a roller that isnt round anymore or a worn out of round roller pin
Could be if you have pressed in studs a stud is slowly pulling out.
Could be a crack in one leg of the rocker that spreads open at high rpm.
If you have dual springs you can easily pass a low speed compression test and have a massive fart at rpm.
Before you chase your tail any further tell us the whole story about the stuck exhaust valve.
 

Anchor

OBS Enthusiast
Joined
Dec 9, 2023
Messages
64
Reaction score
67
Location
Oregon
Hello Thinger; As to the stuck valve, when I trailered the truck home it had no exhaust on it beyond the exhaust manifolds. I hooked the crossover back up and cobbled a muffler on it for noise. Next I did a compression test. 0 lbs in #8. All the rest good. I pulled the passenger side valve cover and started engine and the valve was down and did not move with the cam rotation. I loosened it and pulled out the push rod to inspect. Not bent. When I re-installed it the valve functtioned again. I wondered if prev. owner had maybe tightened the rocker against the valley instead of in the lifter. After pulling it apart I doubt this due to the tiny hole for pushrod. It has never stuck again, that I know of, but I have been dealing with what I perceive as a miss at road speeds. Not at idle. I plan on taking the heads to machine shop this week for exam. I mic'd the cam today, with a cheap digital tool and 1.52 accross the board. Roller lifters look good. Will look carefully at the rockers per your comment on same. Since the rest of the valve train turned out to be Comp Cams the double springs quite possibly are too. I was surprised that when the valve was stuck I didn't detect any noise. I would have thought the roller lifter would be slapping around in the bore and contacting something. Maybe just my old ears. I would never have purchased all of these performance parts but since they are here I would rather get it running and use them. I plan to call comp cams tech on Monday and see if the cam installed would require a new prom card. As to your remark on the studs, when I removed the rockers I have never had the rocker adjusting nut take so much pressure to remove. Better than loose I know but very hard with a 3/8 ratchet. Thanks for your response. I appreciate your input.
 

Anchor

OBS Enthusiast
Joined
Dec 9, 2023
Messages
64
Reaction score
67
Location
Oregon
Kinda guessing it's bigger than .030-over if it's got .040-over pistons.


That can't be good.


Was the flexplate and converter ALSO painted in matching colors? Maybe just a homegrown color code to keep the flexplate and converter aligned.

Or the previous owner's kid was having fun with Dad's spray-paint.
Hi Schurkey; On the bore measurement I used a super dooper digital mic so only approx. but for sure the pistons are marked 0.40 Wondering if the trans bolts to block were causing vibration that I was mistaking for miss? I will look for paint on converter. Didn't realize alignment was critical on converter to flex. But then I don't realize a lot. :) Will post after my heads are checked out. With the valve train that turned out to be installed stock heads seem like a bad fit. Thanks
 
Top