So got it all back together and seems to be running as good as ever. Actually never was running bad only had a few random misfires, Still does.
Here is what has improved.
LTFT were running between +9 to +13
Now with the new Injectors and Intake gaskets, LTFT are running between +3 to -3 Im positive the intake gaskets were leaking causing the higher fuel trims.
Thanks for sharing those great In-Process photos - they are clear enough that folks new to the
old truck hobby can get a good preview of what a Vortec 350 looks like with the intake removed.
Also very cool that you are sharing your fuel trims before/after the gasket renewal + the injector upgrade.
This also made me curious, so I took a closer look at one of your photos. Since the gasketing around the
coolant ports looked good, I zoomed in a bit in order to take a closer look at the witness marks around the
intake ports on your cylinder heads:
You must be registered for see images attach
The way I read it, cylinders #1 & #3 are a good example of what you hope to see around
all 8 intake ports. Especially along the bottom.
Meanwhile, it looks like the intake gasket along the bottom of intake port #5 was at/near
failure to the lifter valley? And I also wonder if a leak test (with a suitable flammable) at
the top of #6 would have shown positive results?
Anyway, you did the right thing by replacing the intake gaskets while in there to renew the
injectors and the previously mentioned seep.
Glad to hear that your powerplant responded positively to the maintenance you performed.
Keep up the good work -and- random photos. Others will benefit by being able to look
over your shoulder like this before addressing a common failure item.